PURPOSES : This study was conducted to derive the optimum mixing ratio of phosphorescent pigment for the development of phosphorescent line marking.
METHODS: In this study, we utilized a literature review and case study methodology, to describe the domestic and foreign state of practice for the production and mixing of phosphorescent pigment for use in line marking. The optimal mixing ratio was derived by comparing the reduction in luminance over time for the various phosphorescent pigment mixing ratios identified in the literature. In addition, performance and construction characteristics were analyzed using field testing techniques.
RESULTS : The results were as follows: 1) the results of the luminance performance standards tests showed that all of the phosphorescence test specimens satisfied the phosphorescent fire protection standard. As the phosphorescent pigment mixing ratio increased, the luminance value increased, 2) the luminance reduction rate was minimum at the mixing ratio of 50%. However, when compared to a mixing ratio 40%, a small difference was recorded, the luminance reduction rate from the mixing ratio of 40% is judged as being converged. Therefore, in view of the economic efficiency, it was determined that the optimal mixing ratio was 40%, 3) as a result of construction on the field, a mixing ratio of 40% was found to have a higher luminance value than the general line marking for up to three hours after sunset, 4) it was found that the phosphorescent line markings without glass beads spraying had a higher luminance value than the phosphorescent line markings with glass beads spraying.
CONCLUSIONS : Through the results of the basic experiments of the line markings obtained by blending a phosphorescent pigment, the results could be applied to play an important role in the development of phosphorescent line marking paint technology and in establishing application planning for on-site construction characteristics.
도로표지용 도료의 품질기준은 KS M 6080의 품질기준을 만족하는 제품들의 경우에도 시공 후 일정기간이 경과한 후에는 도료 자체의 부착력 문제로 교통량 증가에 따른 자동차 차륜에 의한 도료 자체의 마모 손실에 의하여 재귀반사 기능을 부여하는 유리알의 마모 및 탈리로 시인성이 급격히 저하되고 있다. 이에 따른 야간 교통 사고율 증가와 동시에 추가 교통 안전을 위한 부가 보완시공으로 안전시설 제비용이 직접비용으로 유발되고 있으며, 직접비용보다 추가공사로 인한 교통체증으로 사회간접 비용이 증가되고 있다. 특히, 차선의 품질 규격이 KS M 6080 제품에 만족한다 하더라도 빗물의 수막(水膜)에 의한 유리알의 굴절율 차로 재귀반사기능을 하는 차선 도료용 유리알의 기능을 발휘하지 못하여 운전자의 시인성은 열악함을 알 수 있다. 따라서, 국외에서 많이 사용되고 있는 마모성이 우수한 수용성 차선도료, 고성능 융착식 도료, 상온경화형 도료를 도입하여 성능을 비교 검토하였다. 본 연구에서는 차선재료의 내구성 향상을 위해 EN 1436규격에 의한 내마모성 시험을 수용성, 융착식, 상온경화형 도료에 실시하여, 재귀반사도 성능이 우수한 차선재료의 적용 가능성을 확인하였다.