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        검색결과 1

        1.
        2012.10 KCI 등재 서비스 종료(열람 제한)
        T-N and T-P in the filtrate from Sludge Treatment Process (STP) was returned to water treatment processing, because T-N and T-P are returned, it makes overload in Advanced Treatment Process. Removal efficiency of T-N and T-P are compared both at using polymer as simple method and at using PFS and polymer as complex method when coagulants was injected in Thickener. In simple method, removal efficiency of T-N and T-P were 95.68% and 99.29% for each. In complex method, removal efficiency of T-N and T-P were 98.07% and 99.90% for each. From the result, removal efficiency of complex method was highly better than simple method. According to increasing of removal efficiency, returned T-N and T-P loading to water treatment process was decreased (Reduced amount of T-N is 0.2309 kg/hr and TP is 0.0145 kg/hr). Also, the amount of a polymer used has been decreased to 80% by using PFS.