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Bench Scale 구조물을 이용한 TMD 기반 철도역사 진동저감 기법의 실험적 검증 KCI 등재

Experimental Verification of a TMD based Vibration Mitigation Method for a Railroad Station Using a Bench Scale Structure

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복합신소재구조학회 논문집 (Journal of the Korean Society for Advanced Composite Structures)
한국복합신소재구조학회 (Korean Society for Advanced Composite Structures)
초록

Recently, measures for reducing noise and vibration of a railroad station are actively being developed to enhance its property value and comfort level of passengers. In this paper, the applicability of the recently developed vibration mitigation method utilizing a platform TMD (Tuned Mass Damper) by installing a spring-damper system beneath the platform is experimentally verified using a bench scale structure. The two-story bench scale structure is built to simulate a real railroad station, and vibration reduction effect is verified by comparing acceleration before and after applying the platform TMD at the 2nd floor of the structure. The design parameters of the platform TMD system is determined based on vibration analysis result and the MTMD (Multiple TMD) theory recently developed to enhance the effectiveness of the platform TMD method. The vibration is excited to the bench-scale structure using a vibrator. The performance test result for a spring-damper system is also presented. The result of the experiment reveals that the platform TMD method can reduce the vibration of the bench-scale structure by greater than 5dB(V).

목차
1. 서 론
 2. TMD 설계파라미터 결정
 3. 마찰형 스프링-감쇠 시스템의 성능시험
 4. Bench Scale 실험
  4.1 개요
  4.2 실험 방법
  4.3 실험 결과
 5. 결 론
 REFERENCES
 ACKNOWLEDGMENT
저자
  • 문연수(에스코알티에스 기술연구소 연구원) | Moon Yeonsoo
  • 김민수(한국교통대학교 철도융합기술연구소 연구원) | Kim Minseu
  • 이찬영(에스코알티에스 기술연구소 수석연구원) | Lee Chanyoung
  • 지용수(에스코알티에스 기술연구소 이사) | Ji Yongsoo
  • 이규세(선문대학교 토목공학과 교수) | Yi Gyu-Sei
  • 최상현(한국교통대학교 철도인프라시스템공학과 교수) | Choi Sanghyun