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        검색결과 2

        1.
        2023.11 구독 인증기관·개인회원 무료
        KEPCO KPS is the contractor for the full system decontamination (FSD) of Kori Unit 1 and under preparation such as modification, lay out for equipment installation, setting up tie-in/out point for chemical injection and way to pressurize the system, of its successful performance. In this research, KPS introduced how KPS has designed and prepared for the FSD project and how will the chemical decontamination process be implemented. As described in the previous research, chemical decontamination process is planned to be conducted for three cycles and each cycle is consisted of oxidation, reduction, decomposition, and purification. Oxidation and reduction process were conducted at 90°C. Chemical decomposition and purification process were conducted at 40°C due to the damage of IX by the heat. If the decontamination result does not meet the target DF and the dose rate, additional cycle can be conducted. Expected volume of process water for FSD is 200 m3. Three systems have been designated as decontamination targets: reactor coolant system (RCS), residual heat removal system (RHRS), chemical volume control system (CVCS). For the steady flow rate, existed plant equipment such as reactor coolant pump (RCP) will be operated and modifications on some components will be conducted. Due to the limited space for installation, decontamination equipment and other resources are distributed to three different places. KPS designed the layout of equipment installed inside the containment vessel. The layout contains the information of shielding for highly radiated equipment such as IX and filter skid.
        2.
        2022.10 구독 인증기관·개인회원 무료
        In this research, KPS manufactured Full System Decontamination (FSD) equipment, which is consisted of Oxidizing Agent Manufacturing System (OAMS), Chemical Injection System (CIS), RadWaste Treatment System (RWTS), Chemical Waste Decomposition & Treatment System (CWDS) and conducted demonstration test to prepare Decontamination and Decommissioning (D&D) project of Kori nuclear power plant in Korea. Each equipment of FSD was modularized due to the limited size of equipment hatch of Kori nuclear power plant. To simulate the expected circumstances in nuclear power plant such as usage of heater or position of each equipment, additional equipment was used. The chemical concentration and flow rate of process water for FSD were used as mentioned in the previous study by KHNP CRI. FSD was conducted for three cycles and each cycle was consisted of oxidation, reduction, chemical decomposition and purification. Oxidation and reduction process were conducted at 90°C. Chemical decomposition and purification process were conducted at 40°C due to the damage of UV lamp and IX by the heat. Total volume of process water for FSD demonstration test was 2.5 m2. KPS conducted decontamination performance review by calculating thickness reduction and weight loss of installed specimen. Operational review was conducted as if FSD test was conducted in the field based on the result of demonstration test. One of the most prioritized features is the workers’ safety. Also, the appropriate position of equipment needs to be considered to meet the required specification of component.