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        검색결과 8

        1.
        2023.08 KCI 등재 구독 인증기관 무료, 개인회원 유료
        In this study, the change in the mold opening stroke of important functional parts according to the 20, 50, 80, and 100% increase in the injection speed of a hydraulic 150 ton hydraulic injection molding machine was studied to verify the accuracy of the injection speed and mold opening stroke and the reproducibility of the standard deviation. The null and alternative hypotheses were confirmed by conducting hypothesis verification according to the experimental condition change using the experimental design method.
        4,000원
        4.
        2019.12 KCI 등재 구독 인증기관 무료, 개인회원 유료
        In this study, the injection pressure of 31 MPa and clamping force of 1,000 kN toggle electric injection molding machine were used to measure the load transmitted to the frame during injection molding and to use it as the design basis data. In general, the toggle structure is composed of a movable plate, tie bars, crossheads, toggle links, toggle pins, base plates, etc and The material is spherical graphite cast iron(FCD 400). In this study, it was found that there was a 1.3% safety factor by calculating the clamping force in the structure of the five-point toggle link system. In addition, Expected static bottom load, Expected dynamic additional load, Maximum expected additional load, and Maximum weight load were measured using tensile measurements and presented as important basic design data of the assembly.
        4,000원
        5.
        2017.10 KCI 등재 구독 인증기관 무료, 개인회원 유료
        This study is a study on the cracking of the main piston surface which is generated in the injection molding machine to generate mold force. The main piston machining process consists of high frequency heat treatment, grinding and super finishing after lathe turning. Scale, defect size, and fracture texture were observed for four cracks on the surface of the piston during the tempering process after high frequency heat treatment using a metallurgical microscope. In this study, it was confirmed that the cracked structure of the piston structure was ferrite and pearlite structure. It was confirmed that cracks progressed to 480 ㎛ and scale layer of 3 ㎛ or less. Surface hardening layer and hardness were min 2.0mm/HRc 58±2 spec 1.6 mm/HRc 56.5~57.5 In addition, cracks on the surface of the piston appear perpendicular to the rolling process. Therefore, it can be assumed that the crack occurred in the low temperature tempering process at 200°C or less after the high frequency heat treatment, not the material defect. Therefore, the temperature should be maintained at 200°C or higher during tempering after high-frequency heat treatment, and the cracking defect on the surface of the piston can be prevented by setting the feed rate to 1.3 mm/s or less during heat treatment.
        4,000원
        6.
        2016.12 KCI 등재 구독 인증기관 무료, 개인회원 유료
        An injection unit is the important part which guide the melted resine into the mold. Once injection molding is performed, there will be a pressure of 33 MPa built up inside of injection cylinder body. It was confirmed that the crack occurs by internal stress on the 9 mm material when the machine is used for long time. Because the cylinder rod has material thickness of 9~12 mm during manufacturing process on the cylinder body, there would be 3 mm thickness differences. In this experiment, IDEAS, a computer aided structure analysis software, is used to present the optimized design condition. Insert rod with inner diameter of 9 mm was set as a normal and vary 3 mm in x, y axis direction. When the internal pressure of 33 MPa occurs at the injection unit, fix the x and y direction and find out the stress acting only in z axis. It was confirmed that the stress of 45~82 N/mm 2 was built up when the left of cylinder body had been set 9 mm by using a structure analysis. Also, it has been verified the thickness of the material on the left need to be greater and equal than 12 mm to prevent a material crack by an internal stress.
        4,000원
        7.
        2014.12 KCI 등재 구독 인증기관 무료, 개인회원 유료
        In this paper, the 5 joint toggle link of an injection molding machine is optimized. A model considering toggle link kinematics, frictions at the pin joints, and stiffness is verified by a finite element analysis(FEA) and a measured result. The FEA was carried out by the commercial FEA software ANSYS and the clamping force was calculated by measuring the tie-bar deformation of the molding machine. The influence on the maximum clamping force and stroke ratio are analyzed for the length variations of links. Based on the mathematical model and design parameter, the clamping force, the stroke ratio, and the maximum stroke of moving plate are optimized by using the response surface method(RSM) for the length of the toggle link, where the lager-the-better, the norminal-is-best, and the smaller-the-better characteristics are applied for the clamping force, the stroke ratio, and the maximum stroke of moving plate.
        4,000원
        8.
        2014.10 KCI 등재 구독 인증기관 무료, 개인회원 유료
        In this paper, the 5 joint toggle link of a injection molding machine is analyzed. Considering toggle link kinematics and frictions at the pin joints, clamping forces for each cross head position are calculated. The maximum clamping force and the install position of a tail-stock are determined by the stiffness of links, plates and tie-bar. The kinematic results of a finite element analysis considering friction and stiffness are compared with measured results
        4,000원