In this study, flow analysis was performed using ANSYS CFX to evaluate the performance of the 30kg hydrogen fuel cell hexa-copter drone in hovering flight. In the case of a hydrogen fuel cell hexa-copter drone, a total of four cooling fans are mounted on the drone's body in two pairs on the left and right to cool the fuel cell module. In order to evaluate the effect of the air flow from the cooling fan on the aerodynamic properties of the hydrogen fuel cell drone as the mounted cooling fan operates, the change in thrust for the case where the cooling fan operates and does not operate was compared and analyzed. Looking at the analysis results, it was found that the presence or absence of the drone's cooling fan had little effect on the drone's thrust through the thrust results for the six wings.
In this study, a numerical analysis study was conducted on the flow characteristics according to the internal flow path change and differential pressure of the hydrogen shut-off valve, and through this, the pressure loss characteristics and flow coefficient of the hydrogen shut-off valve were predicted. ANSYS CFX program was used to predict the flow characteristics of the hydrogen shut-off valve. When the flow path gap was 1.3 mm, the design conditions of the hydrogen shut-off valve were satisfied, and the value of the flow coefficient of the valve was about 1.53. As the inlet pressure of the hydrogen shut-off valve increases, the outlet flow rate increases, but regardless of the inlet pressure, the flow coefficient of the valve is almost constant, ranging from 1.53 to 1.56, indicating that it is the inherent flow coefficient of the designed hydrogen shut-off valve.
In this study, numerical analysis was performed for the purpose of analyzing the flow characteristics and performance according to the change in the inflow hydrogen temperature and differential pressure of the receptacle of the hydrogen charging system. The pressure distribution and turbulent kinetic energy in the filter area were analyzed by changing the outlet pressure condition under the inlet hydrogen temperature condition, and the flow velocity change at the outlet was compared and analyzed. As a result of the analysis, as the differential pressure decreased, the flow rate at the outlet of the receptacle decreased by up to about 70% at the 2.86 MPa condition compared to the 1.86 MPa condition, and the mass flow rate decreased by about 56.5% at the maximum. It was found that the standard CV performance was not satisfied when the differential pressure at the inlet and outlet was 1.12 MPa or less under the 363K temperature condition.
원자력을 이용한 황-요오드 수소생산 공정 중 황산용액을 이송하는 기존의 시스템과 달리 새로운 황산 이송장치는 벨로우즈 박스 내에서 벨로우즈 외측으로 고온 부식성 액체인 황산이 흐르고, 벨로우즈 내측으로는 냉각수가 흐르는 상태에서 주기 운동을 통해 황산용액이 펌핑 되도록 구성된다. 200 ℃ 이상의 고온 부식성 액체인 황산용액을 정량으로 이송할 수 있도록 장치의 주요부품인 벨로우즈 주변의 열해석을 통해 온도분포를 확인하여, 테프론 재질의 벨로우즈의 내식성 및 내열성을 파악하고, 장치의 안전하고 효율적인 운용을 위한 기초자료를 취득하고자 하였으며, 냉각수 입구직경 3 ㎝, 질량유량이 3.9199 ㎏/s로 고정한 경우 벨로우즈의 길이에 관계없이 테프론 변형온도 이하임을 알 수 있었다.
This study is focused on the channel design of bipolar plate in the electrode of hydrogen gas generator. The characteristics of hydrogen gas generation was studied in view of efficiency of hydrogen gas generation rate and a tendency of gas flow through the riv design of electrode. Since the flow rate of generated gas is the most crucial in determining the efficiency of hydrogen gas generator, we adopted the commercial analytical program of COMSOL MultiphysicsTM to calculate the theoretical flow rate of hydrogen gas from the outlet of gas generator.